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ISSN

2661-3948(Online)

Article Processing Charges (APCs)

US$800

Publication Frequency

Quarterly

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Published

2026-04-03

Issue

Vol 8 No 1 (2026): published

Section

Articles

Technical upgrading and full life cycle economic evaluation of the sulfur shaping unit at Luojiazhai gas field

Hong Yin

China National Petroleum Corporation Southwest Oil and Gas Field Northeast Sichuan Operations Branch

Fang Peng

China National Petroleum Corporation Southwest Oil and Gas Field Northeast Sichuan Operations Branch

Lan Li

China National Petroleum Corporation Southwest Oil and Gas Field Northeast Sichuan Operations Branch

Ran Jiang

Exploration and Development Research Institute, Southwest Oil & Gas Field Company

Xia Luo

School of Economics and Management, Chengdu Technological University

Mengwei Liu

School of Economics and Management Southwest Petroleum University


DOI: https://doi.org/10.59429/pest.v8i1.13412


Keywords: high-sulfur gas fields; sulfur shaping; water granulation process; life cycle assessment; production-sales coordination


Abstract

Addressing issues such as equipment aging, liquid sulfur transportation safety hazards, and insufficient market adjustment capacity in the sulfur recovery system of Luojiazhai Gas Field, this paper conducts a comparative analysis and feasibility study of technical upgrade options for the sulfur shaping unit, using Xuanhan Natural Gas Purification Plant as a case study. By comparing steel belt granulation, drum granulation, and water granulation processes, the technical route for constructing a new 1200 t/d water granulation unit was determined. Based on life-cycle cost (LCC) theory, an economic evaluation was conducted across three dimensions: investment estimates, operational maintenance costs, and synergistic production-sales efficiency gains. Results indicate that while this solution entails higher initial investment than retrofitting existing lines, it fundamentally eliminates long-distance liquid sulfur transportation risks. Furthermore, by implementing a "store during off-peak, sell during peak" strategy, it achieves potential annual efficiency gains of several million yuan. This approach demonstrates significant technological advancement and economic viability.


References

[1] Cai Chunhua, Yin Hong, Peng Fang, et al. Marketing Management Research Under Sulfur Market Fluctuations [J]. Chemical Engineering and Equipment, 2025, (01): 160-164.

[2] Ge Chang, Yu Xiaozhong, Gu Sui, et al. Research on Hydrogen Energy Industry Development in Hainan [J]. Modern Chemical Industry, 2025, 45(S1): 12-16.

[3] Yao Qicai, Yang Jian. Technical Upgrading and Operational Performance of the Conversion Process in a Sulfuric Acid Plant [J]. Sulfur and Phosphorus Design and Powder Engineering, 2025, (04): 44-46+58.

[4]Yang Mengwei, Lin Wuke. Research on the Current Status and Marketing Strategies of the S.ulfur Market [J]. Marketing World, 2024, (22): 74-76.

[5] Ge Chang, Yu Xiaozhong, Liu Mengwei, et al. Current Status and Future Trends of China's Sulfur Industry Development [J]. Modern Chemical Industry, 2023, 43(12): 7-10.



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